Evaluasi Keberhasilan Penanganan Scale Problem Dengan Metode Acidizing di Sumur “Jose-1” Pada Lapangan “Ma-Mandar” Untuk Meningkatkan Laju Alir Produksi

Authors

  • Muhammad Aldi Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan
  • Rohima Sera Afifah Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan
  • Firdaus Firdaus Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan
  • Desianto Payung Battu Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan
  • Dharma Arung Laby Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan
  • Amanda Mustagina Sekolah Tinggi Teknologi Minyak dan Gas Bumi Balikpapan

DOI:

https://doi.org/10.53866/jimi.v1i3.392

Keywords:

Inflow Performance Relationship, Productivty Index, Scale Problem, Acidizing, Stiff and Davis

Abstract

Productivity or commonly called productivity index (PI) in a well will decrease. Marked by a decrease in reservoir pressure (Pr), well flowing pressure (Pwf) and rate (Q) in the "Jose-1" well also decreased due to deposits (Scale) formed in the production zone, thus inhibiting Pr, Pwf and Q. Therefore, the solution that can be done to overcome this problem is well stimulation. The purpose of well stimulation in the "Jose-1" well is to overcome the deposits (Scale) formed so that Q increases. The deposits (Scale) formed can be identified by formation water parameters using several methods, one of which is the Stiff and Davis method with the Scaling Index (SI) parameter obtained. The stimulation method used is the matrix acidizing method, the success parameters of the matrix acidizing method can be seen from the Inflow Performance Relationship (IPR) parameters before and after as well as the PI before and after. This Final Assignment writing is done using manual calculations via excel. Based on the results of the analysis carried out, the "Jose-1" well experienced a decrease in pressure and production flow rate caused by CaCO3 deposits (Scale), proven by the SI value parameters using the Stiff and Davis method where SI> 0 (Tends to precipitate or precipitate CaCO3) which is 1.13 and a skin value of 12.5. After acid injection was carried out on the well, the oil rate (Qo) from 90 bopd increased to 144,539 bopd.

References

Itsnaini, H., Sunarno, S., & Padil, P. (2024). Perbandingan Performa Antara Treatment Hydrochloric Acid dan Carboxylic Acid Terhadap Kenaikan Produksi pada Sumur Minyak Berat. Journal of Bioprocess, Chemical and Environmental Engineering Science, 5(1), 11–18.

Kusrini, D., & Setiawan, M. R. (2022). Evaluasi Keberhasilan Penanggulangan Problem Scale Dalam Upaya Optimasi Produksi Pada Sumur “X” Lapangan “Y”. Jurnal Offshore: Oil, Production Facilities and Renewable Energy, 6(2), 61–67.

Kaliky, I. I. A., Nirmala, G. S., & Pellu, D. I. (2024). Perencanaan Stimulasi Pengasaman Menggunakan Matrix Acidizing pada Sumur IA Lapangan K. Indonesian Journal of Energy & Mineral, 4(2), 99– 107.

Muhammad, R. M. (2020). Perencanaan Program Teknik Stimulasi Pengasaman Menggunakan Metode Matrix Acidizing Pada Sumur FIA PT Pertamina EP Asset 3 Cirebon. Swara Patra: Majalah Ilmiah PPSDM Migas, 10(2), 37–50.

Kusrini, D., & Winarto, W. (2023). Analisa Peningkatan Produktivitas Sumur Menggunakan Metode Matrix Acidizing pada Sumur X Lapangan Y. Jurnal Migasian, 7(1).

Musnal, A. (2013). Mengatasi Kerusakan Formasi Dengan Metoda Pengasaman Yang Kompetibel Pada Sumur Minyak Dilapangan X. Journal of Earth Energy Engineering, 2(2), 1–7.

Bambang Sugeng , MT Pertemuan ke : 1 Pendahuluan. (n.d.). www.aapg.org

Ezquerro, L., Coimbra, R., Bauluz, B., Núñez-Lahuerta, C., Román-Berdiel, T., & Moreno-Azanza, M. (2024). Large dinosaur egg accumulations and their significance for understanding nesting behaviour. Geoscience Frontiers, 15(5). https://doi.org/10.1016/j.gsf.2024.101872

Huda, Amm., Sahara, A., Tinggi Teknologi Migas Jl Transad, S. K., Utara, B., & Timur, K. (2021). Oktober 2021 e-ISSN-2656-5080 Artikel diterima 5. In PETROGAS (Vol. 3, Issue 2).

Jalisar Belo, J., Maulinda Ulfah, B., Jalu Waskita, K., Sera Afifah, R., Studi Teknik Perminyakan, P., Tinggi Teknologi Migas, S., & Studi Rekayasa Geologi, P. (2025). STUDI LABORATORIUM PENGARUH PENAMBAHAN SERBUK KOPI TERHADAP RHEOLOGY LUMPUR DAN FILTRATION LOSS. In PETROGAS: Journal of Energy and Technology (Vol. 7, Issue 1).

Payung Battu, D., Adha, I., Kurniawan, T., Ryka, H., Maulana, D., Eriyanto, I., Studi, P., Geologi, T., Tinggi, S., Migas, T., & Perminyakan, T. (n.d.). POTENSI GEOWISATA DI KABUPATEN PASER, KALIMANTAN TIMUR. In PETROGAS (Vol. 5, Issue 1).

Downloads

Published

2021-12-30

How to Cite

Aldi, M., Afifah, R. S., Firdaus, F., Battu, D. P., Laby, D. A., & Mustagina, A. (2021). Evaluasi Keberhasilan Penanganan Scale Problem Dengan Metode Acidizing di Sumur “Jose-1” Pada Lapangan “Ma-Mandar” Untuk Meningkatkan Laju Alir Produksi. Citizen : Jurnal Ilmiah Multidisiplin Indonesia, 1(3), 164–174. https://doi.org/10.53866/jimi.v1i3.392